Farmall 400 2-71 Repower Project (Step by Step with Pictures)

Update Nov 5, 2018: I’ve made recent upgrades to the engine and have updated this “Step by Step Story” to reflect changes made since my original posting. Basically I ended up with coolant in the oil and head gasket compression seal leakage into the coolant. Modifications were needed. A Discussion of this now appears as a sub bullet article in the menu, 2-71 Head Gasket Issues Experienced and Background Information (https://wordpress.com/page/dieselbobllc.com/827).
Picture Story of the rebuild:






























I primed the fuel system until fuel filters were full and fuel was coming out the return line. The engine fired right up with only a few turns of the crank. The above video is a typical start. I found the used old water pump and fuel transfer pump were both leaking so I have some work to do. A replacement water pump was $782 exchange so have decided to rebuild it myself for about $132 of parts. New fuel pump seals will be about $6.00.
I needed to connect connect the engine throttle lever to the tractor’s driver control lever. To achieve this I constructed a cable system where a 1/8 inch stainless cable runs from the engine’s lever to the lever on the control shaft on the opposite side of the engine through a piece of heavy wall fuel injection tubing The direction on the operator control shaft is reversed,, with up being maximum speed/power.


I plumbed the hydraulic system but had problems with the hydraulic system overheating if I increased the RPM. I added a a pressure gauge and found that at about 800 rpm the pressure regulating system jumped the pressure to around 500 psi and the regulator would not release when RPM was dropped unless I moved a control valve. I concluded this was a problem related to the very large hydraulic pump I had used from the original Allis Chalmers HD5 dozer engine. It took some research to understand the Farmall hydraulic system to decide a course of action.
The Farmall hydraulic system uses closed center hydraulic valves and uses a separate pressure regulating system that is engaged via a 3rd hydraulic control passage to the control valves. When a valve is moved, the low background pressure in the control passage is dropped and the pressure regulator raises the pressure. When the valve is returned to it’s center position the pressure is reestablished and the pressure regulator reduces the working pressure to a low level. With the very high flow rate, of the HD5 pump, the pressure drops across the pump was causing the regulator valve to raise the pressure. I briefly explored the possibility of increasing the size of a control orifice in the regulator block to try to keep the regulating system from malfunctioning, but ultimately decided to find a hydraulic pump closer to the original Farmall pumps size.
The pump I chose is a model GP-F20-25-S9-A from Dynamic Fluid Components Inc. rated at 2900 psi. The Farmall hydraulic system is regulated in the 1200-1300 psi range so the pump provides good factor of safety. I purchased it for $110 from Wholesale Hydraulic Warehouse. The pump has a displacement per revolution of 1.52 cubic inches which I estimate is smaller than the original Farmall pump that appears to be rated at 12 gpm at 1450 rpm (1.9 cubic inch per revolution). This smaller pump would have a flow rate of about 12 gpm at 1800 rpm, where I could run the 2-71 for maximum power, and avoid any chance of the system malfunctioning and overheating.
Installation of the pump required the fabrication of an adapter bracket, the modification of the drive coupling and a resizing to the attachment fittings. The revisions are shown in the following photos.



Latest pictures showing present state of the project follow, sheet metal work to be completed in the spring:

The fast hitch assembly was also in dismal shape and required extensive repair. Besides the normal rust and wear and tear on mounting bracket was broken in two and had to be welded and the one on the opposite side had been previously broken in half and re-welded withe the two halves improperly aligned. Two of the mounting holes had been torched to an oversize to allow assembly without proper support of the bolts. The following slides show how this was repaired by mounting the part, inserting a carbon stick I had threaded with a die into each hole and then welding around the carbon stick to locate the carbon stick. The bracket was removed and the carbon stick reinserted and the balance of the oversized hole was welded shut from both sides, the carbon stick removed, the surfaces ground flat and the hole lightly cleaned up with a die grinder.


In addition to the bracket repair the hydraulic cylinder was rebuilt with new seals and the drawbar, which had been broken in the middle and welded by a previous owner, was reinforced by adding a home built extension plate. This also located the hitch point to the industry standard 14.5 inches beyond the power take-off shaft.


After several months of running I found coolant in the oil and air bubbles in the radiator. Suspecting either a head gasket issue or a cracked head, the head was removed for inspection. Deterioration of the JB Weld Fix of the erosion around several of the water transfer holes had failed, as shown in the above picture. Compression gasket leakage was also observed.



Engine block deck with machined inserts set in place. Each was surface ground for flush mounting. Anaerobic sealant was used under each insert just prior to assembling with a new head gasket. Note, liners and pistons were removed for the modification.

Finished Pictures of the Tractor
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Hi my name is Zach I enjoyed your post very much. My brother and I are Farmall collectors with 19 in the shed as we speek. 400s are by far our favorite. I don’t have the means to do the machine work but I would love to have a m or 400 with a Detroit. Would you consider building a conversion kit or even converting a tractor for me. If not I understand. It would be a great talking piece when we put our tractors on display or pull at our county Fair. Thank you for your time and I hope to hear back from you.
I’ve thought about putting together a conversion kit, but limited time and the question of how big the market is for one has kept me from doing it. I also have an idea on how to do a 3-71. I communicated with somebody at Emerson Matkin, a larger rebuilder and marketer of 2-71’s but there was no interest at the time. I’ll give it more consideration.
I just built a Farmall M with a 2-71 very similar to your conversion, working at a Farmall 706 with a 4-53 Detroit right now, would like to see your Idea for a 3-71 I have a 3-71 setting here looking for something to put it in,
Mike:
I have only done a quick look at what it would take to put a 3-71 in an M or 400. First, the electric fan I used could be easily pushed ahead completely into the shroud. With that done the front face of the 2-71 block would be 13.5 inches away. Adding one more cylinder takes away 5.75 inches leaving 7.75 inches. The rear geartrain of the 3-71 would probably push the engine ahead another inch or two. and the front weight covers on the 3-71 might be a little thicker as well, but the two together should fit within the remaining 7.75 inches. I would assume one could cut down the flywheel housing and mount a plate similar to what I did for the 2-71. The crank end on my 2-71 is about 9 inches from the front bolster casting. Moving it ahead the 5.75 would still leave 3.25 inches and I doubt there would be need to move the engine ahead that much. Water pump is on the side of the 3-71 vs the front mount on the 2-71. On later 3-71s the oil cooler and full flow filter would need to be relocated to avoid frame interference. I’m not sure if the Farmall diesel starter I am using would be big enough for the 3-71. It works just fine for my 2-71, even with the high compression ratio. One could probably rig up a bigger starter if needed.
I don’t know if that would all work – would need to get a 3-71 and measure and explore. A 3-71 easily puts out 100-125 hp and a lot of torque. Probably OK for a show tractor or pulling.
I would like to see pictures of your 4-53 conversion.
Bob
Send me a Email, I tried to post pictures on here but it wouldn’t work
Im in the process of tearing down a 271 from a buckeye trencher. I am planning on doing similar to what you did with either an M or 400. Thanks for posting your detailed process you went through to make it a success.
I can probably give you some more tips and advise, I’ve meant to add some things to my article but haven’t gotten around to it. Where are you located? Feel free to email or call me.
I’ve been in the middle of repowering 400 with a 2-71 and now I came across this link, a little late to the party I guess. Grate job by the way and wonderfull information but I still have a few questions. First is the starter. Original gas engine starter or did you replace it with a 400 diesel? And second what for tach drive do you have on the detroit? These are minor details but any advice on what works keeps me from wasting money and even more valuable time.
I used a starter from a Farmall 400 Diesel. Works very well. Be sure to use a good ring gear. I hadn’t noticed the worn teeth on mine and the starter would often grind and not engage. It was lots of work to replace it – now it engages and cranks every time. For tachometer drive, I drive from the front housing access hole to the lower blower shaft. You can also drive from the rear of the blower if you use a remote filter (like used on the AC HD5 Dozer). Some housing don’t have the access hole in the front housing – just an un-machined boss. It could be machined in. The drive is a right angle one – I have a parts book that has all the part numbers if you need them. Feel free to call me to discuss your project- I can relay mistakes I made and different options.
How it going bob. I have fished my repower project and would like to share some of the final photos with you. It’s not restored like yours but on the same side it’s a work tractor and I ran it for my whole second cutting running dice bine and making small squares. I’m still working some kinks out but I’m very happy with it all around. How can I send you some of these?
Please send them to my email dieselbobLLC@gmail.com. I would certainly like to see them and post.
Bob
Hello, me and my father would like to attempt to repower one of these 400s. Do you have plans or templates for the bellhousing match up and flywheel adapter. Any other advice would be appreciated. We are not looking to to hard work with the tractor just for it to be a trailer tractor and help on our vegetable farm. Thanks -Jed
Sorry to take so long to get back to you. Unfortunately, I didn’t have a layout of the modified plate. What I remember is that to align the plate to the 2-71 housing you had to take careful measurements on the two alignment dowel locations relative to the crank centerline for both the 2-71 and Farmall block and get the 2-71 dowell holes located in the plate. I seem to recall the original farmall dowel holes may have been needed to be welded shut andgrond flat to get the 2-71 holes located properly. Once the parts were dowelled together with the 2-71 housing, I used the 2-71 housing as a guide to drill the other attachment holes.
If I recall, the plate was 1/4 inch and I machined the housing flat with the step the thickness of the plate. I just torched out the 1/4 plate shape to match the 2-71 housing and ground the edge . It was drilled through sandwiched between the mounting plate and the 2-71 housing.
The flywheel adapter plate thickness is a key issue. I made mine out of a 2-71 flywheel as I wanted to have as large a flywheel mass/inertia since the original 2-71 flywheel was larger in diameter. Otheres have machined a smaller steel adapter. I made my adapter a bit too large in diameter and it interfered slightly with a bolt. I needed to use a cap screw and cut down the head on one side for clearance. You can see the cap screw in the 2:00 position on by photo the the flywheel being attached. A critical issue is the adapter thickness to keep the ring gear and clutch face in the proper position. This will depend on the stock removal on the two housing surfaces and any dimensions you can measure from the assembled original Farmall flyheel relative to the attachment plate. I got my flywheel a bit too close to the engine and can tell because of how much clutch adjustment I used up. Also, not shown in my story is a the need to make a spacer between the 2-71 crank and the pilot bearing to keep the bearing from working forward and falling into the larger diameter cavity in the 2-71 adapter plate. I thought the press on the pilot bearing would keep it in place, but after a year or so it worked forward and lost support of the shaft causing clutch problems and noise. Big job to pull engine to fix it!
I can’t thnk of any other advise, feel free to email, text or call me. dieselbobLLC@gmail.com (616)558-7004 (Note:best to text first as I screen calls, or leave a message and I’ll call back.